| <--back larger === smaller standard = high contrast = serif font email me SITE SEARCH |
| home rescued body chassis electric engine transm'n a.t.d.c. |
|
|
| Clutch & Gearbox |
| The gearbox appears to be OK but the clutch is seized solid |
| Mar 04 | After the gearbox cover was removed, the clutch bell housing looked like this: |
| Mar 04 | View of the clutch release bearing oiler. This is the early type with clutch material rivetted to the flywheel and pressure plate. See parts drawing below. |
| Mar 04 | The gearbox was just drained and refilled with SAE40 engine oil. |
| Later - as the gearbox was sluggish with poor synchro when cold, I filled it with Castrol 10W/60 fully synthetic, the same as used in the engine. Result - good sychro on all gears from cold. | |
| Apr 04 | Despite having stood in damp conditions for over 25 years, the clutch freed off with very little persuasion. However there is some clutch spin until a gear is engaged (noisy !)
|
| Jun 04 | ![]() The clutch pressure spring inside the clutch housing; I don't know what that is shining ? - white paint maybe ?Hairy assistant wonders what all the fuss is about ? |
| top of page |
| Aug 04 | Fibreglass gearbox cover from Available Austins was a fair fit but needed some fitting. Long 2BA screws into original threaded holes in gearbox cover plate hold it at the front.a new rubber gearbox cover is now fitted (see new cover) |
| Aug 04 | ![]() ![]() . . . . . and the fitted item, with a close-up of the superb grommet from the Vintage Supplies range. Access to the gearbox filler and the clutch release bearing oiler unfortunately means taking this cover off. |
| Sep 04 | The dragging clutch was a nuisance when trying to engage a gear when stationary. The old trick of touching one of the synchro gears before engaging first didn't work. The covers were removed and the clutch operation watched through the inspection hole. The problem appears to have been the centre plate sticking on the splines (even after oiling), probably due to rust on the exposed part of the first motion shaft. |
| Sep 04 | Picture shows through the inspection hole: foreground: the clutch bearing release oiler (GP6); at the top is the outer rim of the clutch cover (GP19), just above centre is one of the six holes in the driven steel clutch plate centre (GP25). This plate is quite thick and through the hole can be seen one of the flywheel mounting nuts. The pressure plate (GP22) cannot be seen in this view. |
| top of page |
| Sep 04 | Oiling the splines of the clutch plate centre (GP25) had no effect so a little more cunning was applied. First the clutch pedal was fully depressed; the centre plate was prodded with a long screwdriver until it came "unstuck" from the flywheel. When it came free it was very free suggesting that the problem was caused by binding on the splines when the plate was fully forward. It was slid the very short distance back and forwards over its splines (the centre clutch plate itself is springy and gives a little to permit a small amount of overtravel). I filed a slot in the end of a prybar* to fit over the webs of the centre plate so I could slide the plate back and forth with some vigour. A noticeable improvement in the ease of movement was noted after about 10 minutes of vigorous pulling and pushing ! |
| Sep 04 | ![]() * A prybar is a small crowbar - effectively a solid piece of metal with the tip bent at a useful angle for inserting down into the inspection hatch. With the engine running, I can now depress the clutch pedal and watch the centre plate (and with it the gearbox primary shaft) stop rotating. Clutch spin eliminated 100% ☺ It is now so good that I sometimes have to partly release the pedal to rotate the gearbox to engage a gear ! |
| Apr 05 | and to finish it off, new clutch & brake pedal rubbers from ATDC Spares |
| top of page |
| top of page |
| email me | ![]() |